Project Freeze My engine Off (SAAB B207R Supercharged)

evocarlos

Stupid Bollocks
Staff
cleaned up a saab fuel rail (green viton seals) and blocks fitted right not a bodge like my old one
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new 630cc dekas fitted with lube
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extended the exciter wire on the alternator and found a plug that fits
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going back together
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belts a better fit now the alternator is bolted direct to the block
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setting up the injectors in 13 seconds lol
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done
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and its done well sort of
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getting the charging lamp on even tho ive got 14v trying to work out what the problem is im guessing the L pin on the new alternator goes to gnd when running causing the lamp to come on
 

evocarlos

Stupid Bollocks
Staff
new alternator make the davies craig water pump controller go into error mode it dont like more than 14.2v
been p**sing me off since i fitted the alternator
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today it got replaced with the new style that's supportive of 17.5v before overvoltage error
i personlly feel that the new one has much better funcion than the old one the fan test at keyon has gone big plus
it has a warning alarm and when i lock the car and the windows shut the fan dont come on like the old one from the voltage drop
the cooldown cycle is 3mins but works to reduce the system temp 10c before shutting down that dont take that long tbf
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the plx wideband has surprised me today its been in over a year and the sensor health is at 100% after a trip to demon tweaks it normally show 70%
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new toys for the weekend a present to myself for another year older :)
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evocarlos

Stupid Bollocks
Staff
So going on past expectations Carl, this should be fixed by the end of next week, lol. Not good though buddy, any idea how it occurred?
see lower down :)

Gutted for you, was this a z22se block?
no this was the stock 2011 b207r block

Sorry to hear bud:(

What caused the crack and why did the radiator swell so much?
not sure on the crack but the head gaskets been on its way out for a while and the rads expanded for when the bore cracked and the whole cooling loop got 6bar of pressure from the piston even with the crack the pressure was only down 50%
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trying for more power knowing Carl :censored:
as always :)

im feeling for you here carlos
keep your chin up and get back on the wagon

im about to start playing with water injection my self so if you can give any detail it would be appreciated or even a little note here to help others out and having similar issues

http://www.vx220.org.uk/forums/topic/142539-water-injection/
i was advised to fit a small dot1 jet before the rotors and the larger dot3 jet in the inlet after the rotors the system was in and running but had bog down at low rpm(need variable pump controller) and the issue of a poor one way valve at idle (full vac) the valve was passing and emptying the bottle as i was driving at that point i capped the line and stopped filling the bottle i need to look at a solenoid as the vac is to much for the one way valve the car would be mapped then just use a 50/50 mix to combat iat's i dont want to have to rely on the bottle being kept full if its mapped to meth the bottle dont stay full for long it used 3/4 of a tank in a 60mile drive


had a week away at the sea side to clear my head and focus on the plan ahead
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yep got back 2hours later
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out again
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an idea strikes like a lightning bolt
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some work later
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6mm groove cut and bar tapped in place
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all in time to clean the block
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much jet washing later and a bit of sand blasting its came out well for an 80k block
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tfr and water got the brown oil stains off
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front side was still a bit ruff
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oil jets out mains in
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lick of paint to the block and hone the bores
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crank in and sealant applied
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replaced the piston with the broken ring and the mark from the crack
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paint looks good :)
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honing tool did well its put the crosshatch back
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all 4 in and oiled up waiting for the next step
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evocarlos

Stupid Bollocks
Staff
Oh I thought the B207 blocks were meant to be good for about 400bhp :(

Be interested to see how the inserts last (y)

Good to see its going back together already
thats what i thought to hence not pegging this block in the 1st place like the original
the alloy bar should stay fast i gant go anywhere its locked in :) and below the surface
 
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